45 Degree Angle Adapter Defect from David Hudson

David Hudson posted a comment on his experience with the Omni faceting machine’s 45 degree angle adapter yesterday. His comment can be found here:

https://www.omnifaceter.net/another-omni-owners-spindle-and-platen/#comment-23

He forwarded me some photos to back up his text. I’ve copied his comments here as well as posted his photos. As you can see, his nearly-completed stone was totally destroyed when the 45 degree angle adapter literally fell apart.

By hacklebox44 on Mar 11, 2009

Well, the latest fall apart stunt of my OMNIe has just cost me a very nice stone. Yesterday I was cutting a very nice piece of Tanzanian Sunstone. I had the stone complete except for the table, using the 45 degree fixture as I often do I noticed the table wasn’t cutting like it should. All of a sudden the head of the 45 degree fixture fell off hitting the spinning lap and ending up on the floor. I found my stone broken and completely ruined.
Upon checking the fixture to see what the heck had just happened I found the fixture was simply glued together and after near three years of use the glue had dissolved and the fixture fell apart. I talked with two other OMNIe owners that I know and they have had the same problem at one time or the other with their machines.

I must say that quality machining and quality workmanship surely shouldn’t include glueing machined pieces together. Again the quality of this machine has reached another new LOW FOR ME, and I am headed to a local show this weekend to check into the possibility of buying different faceting machine, I am tired of trying to keep this piece of junk running.

Of course this is my opionion and should be viewed as such.

David Hudson

45 Degree Angle Adapter from the Omni Faceting Machine

45 Degree Angle Adapter from David's Omni Faceting Machine

Omni Faceting Machine - Broken 45 Degree Angle Adapter

Broken 45 Degree Angle Adapter from David's Omni Faceting Machine

And here are the unfortunate consequences of David’s 45 Degree Angle Adapter falling apart. If you can imagine the heavy head of the adapter along with a dop and stone attached suddenly falling off the machine and being flung around the lap and across the room, you can understand why the stone ended up the way it has.

My 45 degree adapter with a standard Omni dop weighs an impressive 85 grams. Subtract about 20 grams for the shaft of the adapter and you’ve got 65 grams – more than 2 oz – of brass and stone flying about the room. I expect anyone being hit by that would not be very happy, and being hit in the head or fingers would result in injuries.

The Tanzanian Sunstone destroyed when the 45 Degree Adapter fell apart

The Tanzanian Sunstone destroyed when the 45 Degree Adapter fell apart

Finally, here’s a close-up of the 45 degree table adapter from my own Omni faceting machine. Note the black around the joint where the shaft joins the head. From my early emails with Charlie at Jersey Instruments, he indicated this is pitch used to hold the head in place. Not a press-fit or threaded attachment for such a critical part, but simple pitch.

This part was out of alignment when I first received my Omni, and was among the first parts to be returned for servicing. The “servicing” – which apparently consisted of heating and twisting the dop to the correct orientation – took over 3 weeks. Because I’ve had more pressing issues with my Omni faceting machine, this bit of crappy quality hadn’t made it into the site yet.

As you might guess, my next modification is to either have my table adapter silver-soldered like Dave, or have a new one with a better design manufactured. I’m leaning towards the latter.

My Omni Faceting Machine 45 Degree Table Adapter - note the pitch

My Omni Faceting Machine 45 Degree Table Adapter - note the pitch along the joint

Another View - Omni 45 Degree Table Adapter with pitch holding it together

Another View - My Omni 45 Degree Table Adapter with pitch holding it together

Posted in Blog, Omni Quality? | Tagged , , , | 2 Comments

Another Omni Owner’s Spindle and Platen

There has been a bit of huff and bluster from a certain source lately regarding tearing a “pressed bearing apart on the platten of a faceting machine”. He claims that the Omni faceting machine spindle was pressed into the spindle housing bearings “under 20,000 lbs” and that this removal is the cause of the vibrations that I had complained about.

I think that anyone can see for themselves from the photos in the instructions on Removing the Spindle and Platen that the spindle isn’t press-fit into the bearings with any kind of pressure at all. In fact, when I originally removed the spindle and platen from my Omni faceting machine, it literally fell out of the bearings once I flipped the assembly upside down. I ended up catching the spindle on my lap. So much for 20,000 lbs of press-fit!

As for the vibrations – I have some photos sent to me from another Omni-e faceting machine owner from when he disassembled his spindle and platen assembly. I’ll compare photos with one from my own Omni faceter and then his:

Original Spindle and Platen from my Omni-e Faceting Machine

Original Spindle and Platen from my Omni-e Faceting Machine

Underside of Another Platen from an Omni Faceting Machine

Underside of Another Platen from an Omni Faceting Machine

Platen Underside Close-up from Another Omni-e Faceting Machine

Platen Underside Close-up from his Omni-e Faceting Machine

Platen Underside Close-up from Another Omni-e Faceting Machine

Another Platen Underside Close-up from his Omni-e Faceting Machine

Notice the “high-quality” of machining that was done on his Omni platen – what appears to be saw and coarse file marks on the bottom. While at least mine was machined on a lathe, it appears that his platen and spindle were made from cutting a slice from a bar of aluminum and then mounting that on his spindle!

And at the other end of his spindle, notice the rough hand-filing job done. No finesse or attempt at quality machining here either:

Close Up of his Omni Faceting Machine Spindle End

Close Up of his Omni Faceting Machine Spindle End

You will also notice that on this other person’s spindle there are punch-marks where the bearings sit. Again, an old blacksmith’s trick to make the shaft swell a bit so it fits into the bearing races more snugly instead of machining the shaft precisely to fit the bearing. The Omni-e Faceting Machine is supposed to be a high-precision device accurate to tenths or hundredths of degrees, yet instead of doing quality manufacturing they’ve fallen back to smacking their parts with a punch and hammer to make them fit.

So when our loud friend complains that it’s the owner who’s at fault for the vibrations and problems with their machines, I leave it for you to draw your own conclusions.

Posted in Blog, Omni Quality? | Tagged , , | 1 Comment

Stone #2 on New Quill

I can now safely say that I’m very pleased with the new quill, and that it improves my cutting considerably. This now makes my Omni faceting machine almost worth keeping.

I cut a small Afghan Blue Tourmaline this time, using a modified version of Jeff Graham’s Aqua Cisir design. It’s meant for a 2:1 ratio which my tourmaline was close but not exactly. The design is forgiving enough that this was not a serious issue.

As you can see from the photos below, the meets are pretty darned good. Much better than I’d been able to achieve previously on the stock Omni quill, and with much less cheating. I think I only had to cheat less than 1/4 of a division on the cheater at the polish stage – unheard of as i was using a full turn or more of the cheater using the stock quill.

I should point out that my results are cumulative of aligning the rest of the machine first, and now this quill is what seems to have pushed the Omni into an acceptable accuracy. However I have the following advice to anyone who owns an Omni:

  1. Align your mast asap. This will reduce the alignment problems that come from the mast being off-vertical.
  2. Tighen the Swing Arm to the point where it is difficult to move. This will reduce the amount of flex in the swing arm caused by compressibility of the plastic disks used as bearings.
  3. When cutting put a pencil mark on the Swing Arm to remind you of the position it was in. This is important because every time you move the Swing Arm you are changing the alignment of the stone to the lap due to all the accumulated inaccuracies in the Omni’s construction.
Close-up of Crown Meetpoints

Close-up of Crown Meetpoints

Close-up of Pavilion Meetpoints

Close-up of Pavilion Meetpoints

Finished 1.55 ct Afghan Blue Tourmaline 1

Finished 1.55 ct Afghan Blue Tourmaline 1

Finished 1.55 ct Afghan Blue Tourmaline 2

Finished 1.55 ct Afghan Blue Tourmaline 2

Finished 1.55 ct Afghan Blue Tourmaline 3

Finished 1.55 ct Afghan Blue Tourmaline 3

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New Stainless Steel Collet Quill

I received my new stainless steel collet quill just before New Years and finally had a chance to install it and test it out. I received 2 quills, one of which was installed in my yoke. You can read about the problems I discovered with the original Omni faceting machine quill on my Another Frustration – Quill Runout post.

Here is a photo of the collet quill installed on my Omni.

New Collet Quill Mounted on the Omni-E Faceting Machine

New Collet Quill Mounted on the Omni-E Faceting Machine

There are a few things to note:

  1. Being a collet design, there is no set screw to hold the dop in place.
  2. There are two dimples machined into the shaft of the quill. These are to accept a special wrench to give a bit better grip for tighening the collet.
  3. This is precisely machined to be a tight friction-fit into the index yoke bearings. This means no screw holding the quill in place, and no possibility of quill wobble in the bearing races like the original design.

Here are some comparison photos with the second quill. It does not have the dimples in the shaft and the collet nut is a slightly different design, but otherwise the quills are identical.

Original Brass Omni Quill and New Collet Quill Side by Side

Original Brass Omni Quill and New Stainless Steel Collet Quill Side by Side

Original Brass Omni Quill and New Stainless Steel Collet Quill Back View

Original Brass Omni Quill and New Stainless Steel Collet Quill Back View

The quill has been so precisely machined to fit the quill bearings that you can’t just slide it into place. In order to get the new collet quill to fit into the Omni faceting head, you need to throw it in the freezer for 20 minutes so it contracts slightly. With a bit of light grease on the bearing races you then quickly push it into place and voila, it’s ready to use. As it warms up it forms a very tight fit into the bearings.

Cutting Results

So of course everyone wants to know the meat of the story: how does this new collet design quill cut?

First of all – it’s 8x more accurate than the original brass Omni quill. The original quill had 0.0055″ of runout when measured at the machine shop. The new quill was measured to have under 0.0007″ runout. Now that’s getting close to what it should be. Under 0.001″ at very least.

To test it out I decided to try a cut that would have had me pulling my eyes out had I tried it on the old quill. My biggest complaint was that cutting square step cuts was a nightmare as nothing seemed to line up enough to get decent meets. This is not a surprise once I realized that the quill had an immense wobble about the dop axis. So I chose to modify Ernie Hawe’s Asscher design (from the USFG List files section) which is nothing but steps in a cut-corner square shape.

The verdict? It’s a huge improvement over the original quill. I still can’t cut to depth using the angle meter as there’s still some slop in the system somewhere which is throwing the depth off a bit, but it’s way closer than before. This stone took a total of 5 hours from dopping to completion – much less than I expected.

There was much less need to use the cheater, and the meets actually fell into place with very little tweaking! This is a first for me cutting on the Omni faceting machine – I just couldn’t get proper meets with the stock parts and crappy transfer jig. And I’ve been an Omni owner for 18 months.

I’ll let the photos speak for themselves. Here are some pictures of my test cut peridot. It has a couple of lilypad inclusions in the pavilion and crown, plus a small internal fracture. But the brilliance and play of light in the stone pretty much hides the defects.

Close-up of pavilion facet tiers

Close-up of corner pavilion facet tiers

Close-up of pavilion facet meets

And here you can see the finished gemstone: 1.60 carats, 6.3 mm square San Carlos Peridot

Asscher Cut San Carlos Peridot 1.60 carats

Asscher Cut San Carlos Peridot 1.60 carats

Sorry, I no longer have any of these custom collet quills left for sale and do not have any leads on where to get one machined.

Posted in Custom Collet Quill | Tagged , | 2 Comments

New Quill Pictures

Well, unfortunately due to the holiday rush and extreme weather we’ve been having on the West Coast, I didn’t get the new quill in time for the break. I’m disappointed but given the weather – we’ve got 2-1/2′ of snow on the ground in a city where 1″ of snow is a big deal – it’s unavoidable. I’ve been house-bound for the last 8 days as my car can’t negotiate the snow in the alley and is getting high-centered as it plows under the bumper.

Anyhow, here are some pics of the new quill from Mike. Pretty space-age in appearance, and he measured less than 0.0007″ runout at the tip of the dop. Now that’s much better than the original 0.0055″!

I hope everyone is having a good Christmas break!

-Allan

Collet Quill with Wrenches for Tightening

Custom Stainless Steel Omni Collet Quill with Wrenches for Tightening

Custom Omni Quill with Proper Press-Fit into Bearings - No Wobbly Machining!

Custom Omni Quill with Proper Press-Fit into Bearings - No Wobbly Machining!

Custom Stainless Steel Omni Quill with Collet - under 0.0007 runout at tip of dop!

Custom Stainless Steel Omni Quill with Collet - under 0.0007" runout at tip of dop!

Posted in Blog, Custom Collet Quill | Tagged , | 7 Comments

New Design Quill Update

Just updating the site so people don’t think I’ve forgotten.

I’m hoping to get my new stainless-steel collet quill before Christmas. Mike has been overloaded with work and since this isn’t a rush it’s been on the back-burner.

Once I get it I’ll post some photos then I’ll cut a couple of stones and let you know how it works.

I’m looking forward to it!

-Allan

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Quill Disassembly Instructions

I’ve just posted my instructions on how to Remove the Quill from your Omni Faceting Machine.

This is the first step required if you want to replace your Quill with another.

Enjoy!

-Allan

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Omni Quill Disassembly

So after all this time, why would I suddenly decide to take my Omni Faceting Machine’s most delicate components apart? If you’ve been following my Blog entries you’ll remember the Another Frustration – Quill Runout post.

To be to the point – I was alerted by others to yet another manufacturing defect and quality control problem with the Omni Faceting Machine. After experiencing the same sorts of frustrations cutting stones and finding the machine out of alignment, other Omni owners noticed that the Quill wobbles about the long axis. In other words, it doesn’t spin true and has a large runout.

Others have told me they have measured 0.0055″ to 0.0075″ runout on their quills. I have measured 0.0035″ runout on mine, and now I understand why I have such problems with cutting by sound or by the angle-indicator. Depending on what index position you’re cutting, the Quill will be closer or further from the lap than another index position!

To put it in perspective, the Polymetric Scintillator states that their Dop Arm (Quill) is adjustable to 0.0002″ Total Indicated Runout. This is between 17.5 to 37.5 times more accurate than the Omni measurements I’ve received!

In my opinion, any Quill runout of more than 0.001″ is unacceptable.

I decided to take my Faceting Head apart to see if there was any way to adjust the Quill runout. There is not.

First Step

To get at the screws mounting your Quill to the Omni Faceting Head, you will need to remove the Index Wheel.

Lock the Index Pin up so the Quill is in free-wheel mode. Using a slot screwdriver, carefully remove the two screws holding the Index Wheel in place. Gently ull the Index Wheel and slide it off the Quill. It may need a bit of WD-40 to loosen any corrosion and rock dust so it can slide off the Quill. Be careful not to pull the little bead off the end of your Index Pin.

Omni Faceting Head showing Index Wheel screws

Omni Faceting Head showing Index Wheel screws

There is a brass ring which the Index Wheel screws into. You can remove this from the Quill by loosening the Allen screw holding it to the Quill and slide it off also.

Your Faceting Head will now look a bit naked, like this:

Omni Faceting Machine Quill with Index Wheel Removed

Omni Faceting Machine Quill with Index Wheel Removed

Removing the Quill Assembly

Using the appropriate size of Allen key, undo the 3 screws holding the Quill and Yoke to the Faceting Head.  Be careful as the last screw is removed – the Index Pin is spring-loaded and will push the Yoke. You don’t want to drop this part!

Carefully remove the Index Pin Spring and put it somewhere safe with the Allen screws.

Your Quill and Yoke assembly is now free of the Faceting Head.

Omni Faceting Machine Quill and Yoke Assembly

Omni Faceting Machine Quill and Yoke Assembly

The Quill

As you can see, the Quill is held into the Yoke by a bearing and a screw in the back of the Quill. I removed the screw. You can see the screw has some sort of Locktite on it to prevent it from loosening on its own.

Omni Faceting Machine Quill and Yoke Assembly with Screw Removed

Omni Faceting Machine Quill and Yoke Assembly with Screw Removed

About here I had the shock of my life – as I picked up the Quill and Yoke assembly, the Quill fell out of the bearings under its own weight! I had fully expected the Quill to be press-fit into the bearings to ensure that the Quill didn’t wobble in the inner race. I was wrong.

In this picture you can see the base of the Quill where it fits into the bearings. Notice that there are no scratches or other marks from when it fell out of the bearings – it sits in there loosely. How one can expect to have a precise alignment when the shaft does not fit tightly to the bearing is beyond me.

Close-up View of the Quill base

Close-up View of the Quill base

The Yoke

I’ll resist saying “the Yoke’s on you”… or maybe not 😎

The Yoke has two 6000RS bearings which the Quill slides into. What you can’t see from the photo is that the two 6000RS bearings are not just press-fit into the Yoke body but they’re resting against a fin of metal machined into the Yoke between the two bearings.

This means you’re not going to be able to replace the Yoke bearings very easily, if at all. I had to get my machinist make a special tool to pull them out so I could replace them with some higher-tolerance ABEC-3 rated bearings. I was told that this was a very difficult process.

Omni Yoke showing the pair of 6000RS bearings

Omni Yoke showing the pair of 6000RS bearings

Here’s a view of all the parts of the Quill and Yoke assembly together.

Omni Quill and Yoke Parts

Omni Quill and Yoke Parts

My Custom Quill Design

After some discussion with the other Omni owners and the machinist, I have designed a replacement quill to be made out of Stainless Steel.

Brass does not have very good properties for retaining shape – so if you accidently bang it or somehow flex the thing, it’s not going to spring back but stay in the new shape. Stainless Steel will bounce back, plus it’s much harder and stronger.

An excellent suggestion from one of the other owners was to make the Quill with a collet to hold the dops rather than a set-screw. This does two things – it makes it easier to put the dops in and out (no mis-placing the bloody Allen key) and it helps keep the dops centered even when they are a bit worn.

The Quill is still being fabricated but as soon as I get it I’ll be posting photos. I have asked to have a few extra made up (the cost is mainly in getting the machines set up, not in producing the pieces) so if you want to replace your brass quill with a stainless steel collet quill I can sell you one.

In the mean time I’m eagerly waiting.

Posted in Removing the Quill | Tagged , , , , | 4 Comments

My Custom Omni-E Splash Pan

Here’s a quick pictoral guide to how I created my $5 custom splash pan for my Omni-E faceting machine. This is a more detailed set of pictures and instructions than in my blog post $5 + 2 Hours = New Splash Bowl.

Please remember that I’ve modified my Platen so it is now 4″ in diameter, not 6″. This is key as it will determine what you will use to create the new Splash Pan.

You will need to remove your existing Splash Pan – follow the instructions in my Removing the Platen and Spindle and Removing the Splash Pan posts.

Get the Parts

First, go find yourself two plastic containers – I went to the local Dollar Store and found a nice big plastic bowl that was about 10″ in diameter on the inside. The other container was a pasta container (similar to a 1 quart yogurt container) that was about 5″ in diameter. I also picked up one of those thin flexible poly vegetable cutting mats.

And then I went to the local Medical Supply shop to buy a foot of the thickest rubber exercise bands (“Theraband”) material I could find. This rubber and the cutting mat will become the splash pan cutout thingie. You will also need some Silicon Sealer plus some sort of drain tube.

I used the following:

  • 10″ Diameter Plastic Bowl (from Dollar Store)
  • 5-1/2″ Diameter Pasta Storage Container (from Dollar Store)
  • Poly Cutting Mat (from Dollar Store)
  • 1 foot of Theraband rubber (from Medical Supply shop)
  • 6″ of 5/8″ Diameter Surgical Tubing (from Medical Supply shop)
  • Black Silicon Sealer
  • Body of a thick plastic pen (to be explained later)
Plastic Bowl

Plastic Bowl from the Dollar Store

Pasta Container

Pasta Container from the Dollar Store

Theraband and Cutting Mats

Theraband Elastic and Cutting Mats

Make the Collar

Cut the pasta container so that it now fits easily over your Platen with at least 1/4″ to spare around it. Put this over top of your Platen so you can now see how tall to cut it. Mark it with a pen and then cut it to create a nice collar that ends about 1/8″ or so below the bottom of the Platen.

Pasta Container Cut to fit Omni Platen

Pasta Container Cut to fit Omni Platen

Pasta Container Cut Just Below Platen

Pasta Container Cut Just Below Platen

Fitting the Collar to the Splash Bowl

Now that you’ve got the collar created, it’s time to cut the bowl so it fits.

I used a drafting compass with the pencil lead replaced with a second pin to scribe a circle slightly less than the outside diameter of the collar in the bottom of the bowl. I then carefully cut the bottom bit out of the bowl.

Disembodied Hand Scribing the Bowl

Disembodied Hand Scribing the Bowl

Bowl Bottom Cut Out

Bowl Bottom Cut Out

Using a wood file I carefully enlarged the cutout so that the collar could slide half-way through the opening. I left a little more than 1/2″ of the collar sticking out of the bottom of the bowl.

Bowl with Core Inserted

Bowl with Core Inserted

I now cut the bowl down to a reasonable height – total height of Collar plus Bowl is about 4″ – so I cut the bowl down to be 3-1/2″ from bottom to the new lip. When taking this photo I nearly cut myself!

Cutting the Bowl to Proper Height

Cutting the Bowl to Proper Height

Collar and Bowl Together

Collar and Bowl Together

Now to test the whole assembly before silicon sealing the whole thing together:

Make the Drain and Seal Together

I forgot to do this step until after I sealed everything together. Probably the wrong time to do this!

Figure out where you want your drain tube to come out and at what angle. For me, I needed to have it come out the back of the new Splash Pan at an angle so it wouldn’t interfer with the way the assembly sits on my Omni faceting machine.

I used the barrel of a very ugly and fat plastic pen to create the drain. Carefully cut a hole near the edge of the bowl so that the tube you use will stick out at the correct angle – it will be oval or marquise-shaped depending on the angle you want it to come out. Carefully file the hole so the tube fits reasonably well.

Now carefully use the silicon to glue the collar and bowl together. Set aside to dry a bit – at least an hour so the sealer skins over and you won’t knock the thing apart handling it.

Now get out the Silicon Sealer and goop silicon around the drain tube and hole to hold it in place. Don’t forget to seal the inside of the bowl too – but be careful to leave it flush with the inside of the bowl. Let the whole thing dry overnight. (BTW – I didn’t let it dry before continuing. I ended up having to re-seal everything later)

Splash Pan Drain Tube

Splash Pan Drain Tube

Splash Pan Drain Inside View

Splash Pan Drain Inside View

Make the Girdle Cutout and Splash Guard

Once the new Splash Pan assembly is dry, set it over the Omni Platen. Put a lap on your Platen and then using a marker, draw a nice girdle cut-out slot on your new Splash Pan. Be sure to make it 3-1/2″ wide at the bottom so that you have enough space to swing the dop but not so large that water will spray everywhere. I made mine 4″ wide.

Carefully cut the opening. I used smooth curves so that the plastic wouldn’t crack or break at the cut corners.

Make the Girdle Cutting Slot in Splash Pan

Make the Girdle Cutting Slot in Splash Pan

Now take the poly cutting mat and stick it into the Splash Pan somewhere other than the Girdling slot. Hold it against the inside of the bowl and use a pen to mark where the top of the bowl is. Remove the mat. You now have a nice arc that will match the edge of the Splash Pan.

Girdle Splash Guard Step 1

Girdle Splash Guard Step 1

Girdle Splash Guard Step 2

Girdle Splash Guard Step 2

Mark out the size of the girdle splash guard on the plastic mat. Cut two identical pieces from the poly mat, then put one of them in the Girdling Slot you cut so that the top of the piece is just above the girdle cut-out. Mark this line.

Girdle Splash Guard Cutout 3

Girdle Splash Guard Cutout 3

The rubber Theraband is going to be a soft bumper on the top of the Splash Guard. Cut a strip of the Theraband about 1-1/2″ wide the length of the plastic strips. The Theraband is to be folded and sandwiched between the two poly sheets.

I can’t think of a way to describe what to do next, so I’m just going to show you the pictures of what you’re supposed to do. I used staples to hold the whole mess together and then put some silicon over the staples so they wouldn’t rust. This has proved quite effective and has not fallen apart or loosened up yet.

Girdle Splash Guard Step 4

Girdle Splash Guard Step 4

Girdle Splash Guard Step 5

Girdle Splash Guard Step 5

Girdle Splash Guard Step 6

Girdle Splash Guard Step 6

In this last picture I’ve trimmed the Splash Guard and glued the loose flap of Theraband to the plastic with silicon sealer.

Girdle Splash Guard Step 7

Girdle Splash Guard Step 7

Water Drip Cutout

The final step is to create the cutout so the water drip spout can move and sit properly. Put the new Splash Pan on your Omni faceting machine and mark where the drip spout needs to go. Cut this out.

Here are two pictures of the completed splash pan without the Girdle Splash Guard and with it in place.

Water Drip Cutout

Water Drip Cutout

Water Drip Cutout with Girdle Splash Guard in place

Water Drip Cutout with Girdle Splash Guard in place

Oh, and don’t forget to put the tubing on the end of the water drain tube before you use this!

My new Splash Pan can hold bowl more than the contents of one full water drip container without overflowing! Mind you, at high speeds the wind from the laps will cause the water to rotate and then it will overflow, so I don’t suggest using this Splash Pan without the drain.

Enjoy! Let me know how your splash pans turn out!

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Quill Runout Update

It’s been a while since I have had some time to work on the site. During the past few weeks I’ve taken apart my Omni faceting head and photographed it. I will be posting photos of the process hopefully in the next couple of days.

I also have had a machinist look at the quill assembly to see if he could find what was the cause. His response was that there was a quality problem with the way the quill was made. It was not measured after machining as they assumed the lathe was cutting correctly. It was not, which explains why the others who have found this problem with their own Omni faceting machines have almost the identical runout amount and directionality.

The other issue with the quill is that it’s supposed to be friction-fit into a pair of bearings in the faceting head. However when I loosened the screw holding the quill into the bearings, the quill literally slid out of the bearing races under its own weight! With proper press-fitting of this part there is no way you should be able to pull it out of the bearings by hand, let alone have the part slide out on its own.

As a result of some discussions with the other owners, I am working with Mike to design a collet-based quill that will do away with the set screw. This should ensure that the dops are held perfectly centered in the quill despite any wear of the dops or quill that may occur over time.

The new quill will be made from stainless steel, which has better mechanical properties to ensure that the alignment will be maintained over the long-term.

Once I have the design finalized I will be buying a several of these collet-based quills which I will offer for sale to other Omni owners. It’s significantly cheaper per piece to buy several made at once rather than a single item.

*Note – I am no longer able to get these custom quills

Stay tuned!

-Allan

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